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高效失水堵漏剂在塔河油田二叠系的应用
引用本文:黄贤杰 董耘. 高效失水堵漏剂在塔河油田二叠系的应用[J]. 西南石油大学学报(社会科学版), 2010, 29(4): 159-162. DOI: 10.3863/j.issn.1000-
作者姓名:黄贤杰 董耘
作者单位:1.中国石化西南局重庆钻井液公司,重庆 400042; 2.中国石油川庆钻探分公司川西钻探工程技术服务公司,重庆 400042
摘    要:对S119-3井井深5115m石炭系储层作承压堵漏试验,经过4次惰性材料桥塞堵漏未成功,改用高效失水堵漏剂HHH与清水配置堵漏。该剂具有高效、高失水、高强度等特点,但在配置高密度堵漏浆时,存在悬浮能力差,失水量快,一旦静止很容易沉积于罐底、管线和钻杆中;当堵漏浆与井壁接触,迅速失水、泥饼增厚、结块、易卡钻具。通过实验调整CMC加量为0.15%,提高堵漏浆悬浮能力和延缓其全失水时间。大样全失水时间较长,超过预期控制全失水时间40~60min,大样120min没有完成失水,达到堵漏设计中施工时间要求。实际1.46g/cm3的堵漏浆没有沉淀和堵塞管道,堵漏获得成功,为后期施工井堵漏提供了可靠的依据

关 键 词:高效堵漏剂   悬浮能力   全失水   堵漏   塔里木盆地

THE APPLICATION OF THE HIGHLY EFFCTIVE LOST CIRCULATION ADDITIVE IN THE PERMIAN IN TAHE OILFIELD
HUANG Xian-jie DONG Yun. THE APPLICATION OF THE HIGHLY EFFCTIVE LOST CIRCULATION ADDITIVE IN THE PERMIAN IN TAHE OILFIELD[J]. Journal of Southwest Petroleum University(Social Sciences Edition), 2010, 29(4): 159-162. DOI: 10.3863/j.issn.1000-
Authors:HUANG Xian-jie DONG Yun
Affiliation:1.Chongqing Drilling Fluid Corporation of the Southwest Bureaus SINOPEC,Chongqing 400042,China;2.Western Sichuan Drilling Engineering Service Company of Chuanqing Drilling Company,CNPC,Chongqing 400042,China
Abstract:The pressure sealing test is carried out to the Carboniferous reservoirs of well S119-3 at the depth of 5115 meters,after four times of unsuccessful inert material bridge plug sealing,highly effective loss circulation additive HHH combining with fresh water is applied to seal.The additive is of the characteristic of high effect,high water loss and strong leakagesealing,the analysis of high density sealing slurry indicates that its suspending property is poor,water loss is fast and the slurry is easy to deposit to the bottom of tanks,pipelines or in drilling pipes while resting,when the slurry contacts the well bore wall,water loss occurs quickly,mud cake increases in thickness,chunks are formed and the drilling pipes are easily stuck.By experimental adjustment,the amount of CMC is increased 0.15%,the suspending property of sealing slurry is enhanced and the full water loss time is delayed.The time for full water loss is longer,40~60 min more,in 2 hours,water is not completely lost,the requirement for operative time in leakage sealing design is met.The 1.46g/cm3 leakage sealing slurry does not precipitate and plug pipes,the operation is successful.
Keywords:highly effective lost circulation additive   suspension ability   full water loss   leakage sealing   Tarim Basin
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